If you want a step by step of the RIGHT way and order (as well as avoiding the "oopses" I made) see this file before reading this one! http://home.rmci.net/gregg1/HF-vise2.txt The 4" vise that comes with the Harbor Freight 12-speed Mill/Drill is a solid hunk of iron, but it isn't what I'd call accurate. So I decided to change that. The first problem is that it's not possible to use a parallel against the fixed jaw because the ways do not go all the way to it. Accuracy for this step isn't critical so remove the fixed jaw's face and mill across the vise throat between the end of the ways and the jaw. Be sure to get close enough to the jaw so that the face will overhang the slot when it's replaced. Replace the face and using your parallels, mill a chunk of aluminum or steel to the width of the slot. Mill the face of the bar that will be down against the vise base so it's fairly rough. (Use a faster feed speed.) Drill then countersink a hole for a flat head Phillips machine screw through the center of the face of the bar opposite the side that will be down. You want the screw deep in the bar because you don't want to mill off the head. Now place the bar in the slot and spot drill using the same bit you used to drill the hole through the bar. Switch to a bit appropriate for tapping threads to fit the machine screw, then tap the hole. Cast iron is easy to tap. Make sure the hole is deep enough so that the bar can be bolted down very tight! Carefully clean the metal bar and the vise throat to remove all grease and oil. Mix up and smear some J-B Weld* on the bottom and long sides of the bar and also on the screw threads and underside of it's head. Place the bar in the slot and bolt it down TIGHT so the J-B Weld oozes out all around. Let it cure overnight. *Often called Araldite in the UK and some other countries. Moglice or other "plastic steel" should also work. This is now where I made a "process error". :p I milled the aluminum bar "flat" to the vise ways and also took a TINY bit off the ways. I carefully allowed the mill to just set under it's own weight onto the way then tightened the quill. The mill will then remove a very small amount of metal. I got it all nice and flat but when I turned the vise back perpendicular to the table it "leaned" one direction .001" over the width of the vise. (Figured by measuring a chunk of aluminum milled on two "parallel" edges.) Ouch! I should've known the various parts of the vise were probably not quite true. :( OK, time to do what I should've done to start with. Remove the vise from its base and use a punch to knock the pivot pin out of the center. Use a file on the bottom of the base and smooth down the various bits that poke up and watch how all the edges smooth faster, indicating they're higher than the supposedly flat areas of the bottom. I just got it to the point where all the edges were brightened up and called it good. Bolt the base to the mill table and use the gentle set on technique to mill the top of the base until it makes a cut over the entire area. It should now be flat and parallel to the table, providing a GOOD foundation like a vise should have! I filed the bottom of the upper part of the vise like I did the bottom of the bottom. Then I made another "process error". :( I removed the base from the table to insert the T bolts, mounted it back on the table, punched the pivot pin back in and mounted the vise top back on while failing to notice that it "rocked" a bit. I milled the top of the ways and the aluminum insert until they were flat again, marveling at how terribly un-flat the top of the base had been. I discovered my "oops" when I turned the vise 90 degrees. I could visibly see that it wasn't right. :( I removed the nuts and spun the top around and noticed that it would rock back and forth a bit. That's when I remembered that the center of the base around the pivot pin was quite a bit lower than the two outer rings! Out came the pin and I cut three light passes off the center boss. Pin back in, top back on and it set flat on the outer rings! So I milled the top of the ways AGAIN. They were VERY much not flat. But now they would be very close. This is when the idea hit me of what I should've done at the very beginning, before milling the vise throat and after milling the top of the base flat. I flipped the vise top upside down so the ways were setting on the table. To clamp it down I used the two square washers that were on the bolts holding the mill to the crate base. They fit pefectly on the bottom of the ways and held it tight with the outboard ends propped up on some nuts. Next I milled the bottom of the vise top flat and parallel to the topside of the vise ways. To reach all of the bearing surface you must hang the fixed jaw over the back of the table and swivel the head off to one side some. Position the vise top so that the table can tavel enough to clear the mill off both sides at the centerline where the pivot hole is. There's just enough fore/aft travel to cover the bearing surface using an 11/16" end mill. (Use 3/4" if you have a 3/4" holder.) NOW is when you should re-assemble the vise, mill the throat, make and bolt/glue in the metal bar then mill down the bar and LIGHTLY mill the top of the ways. If all went well it should only need one pass over the ways. If you follow the _proper sequence_ like I didn't, you should be all done. :) What I have to do now is figure out how to hold down the movable jaw so that I can mill off a bunch of the sufaces where the retaining bars mount. For some reason I seem to have a lot of clearance there. No idea why. ;) The movable jaw has two surfaces on the top where it's obvious that it was rested on a milling table when the machine work was done on its bottom side. I'll remove the jaw face and go from there. If I get extra ambitious I'll get a cup wheel and regrind the top edges of the jaw faces so they'll be level with each other again. At least the vise will be (hopefully) far more accurate than it was originally. It does turn much easier now. To aid that I'm going to drill out the very crude pivot hole and press in a bushing that's a lot better fit to the pivot pin. Have fun accurizing your 4" Harbor Freight Milling Vise (or any cheap milling vise) and don't make the same "process errors" that I did! :) Addendum: I've bored out the pivot hole in the top with an 11/16" HSS end mill which poked right through almost like the cast iron wasn't there. Then I turned down a bit of steel tube to .001" oversize and pressed it in with some J-B Weld Kwick to make sure it stayed out. I left a bit of the tube sticking up and turned a bevel on the inside to help locate it under the 9/16" end mill I used to bore a nice, straight and smooth hole. That done, I used a hacksaw to lop off most of the sticking out part then milled off the rest. Finally, I turned down the original pivot pin for a nice fit in the steel bushing. Spins like a dream now. Had I really wanted to, this would've been a great time to ensure that the pivot point was right in the center of the vise top, but given that the scale on it could hardly be accurate and on the drill/mill the base has to mount at an angle it's useless anyway. Finally, I've milled off the bottom of the movable jaw a bit. The two ways are a bit different thickness so each side of the jaw needed a different amount carved off to make it snug. The bearing surfaces took one light pass to level them up because there was a high end at the back on one side. The last thing to do is mill or grind the tops of the jaws so they'll be the same height and level.